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    高等级焊管用316L不锈钢冷轧板焊缝浮渣缺陷改进方法

    Improvement method of weld slag defect of 316L stainless steel cold rolled plate for high grade welded pipe

    • 摘要: 针对医疗领域高等级焊管用不锈钢对焊缝的高质量要求,分析了常规生产的316L不锈钢冷轧板焊接后焊缝出现不同程度浮渣且影响实际使用的原因,对不同S元素含量的316L不锈钢冷轧板开展对比焊接试验。结果表明:焊缝浮渣主要是由Al2O3-SiO2-CaO复合型夹杂物上浮至熔池表面后凝固形成的;增大熔池深度可抑制夹杂物上浮至表面后形成浮渣,而增大能改变表面张力温度梯度的表面活化元素S元素的含量,能够使熔池表面张力温度梯度呈正值,进而形成更深、更大的焊接熔池。

       

      Abstract: In view of the high quality requirements of stainless steel for high-grade welded pipes in the medical field, the causes of different degrees of slag in the weld of conventionally produced 316L stainless steel cold-rolled plates after welding and its influence on the actual use were analyzed. The comparative welding tests were carried out on 316L stainless steel cold-rolled plates with different S element contents. The results show that the weld slag was mainly formed by the solidification of Al2O3-SiO2-CaO composite inclusions after floating to the surface of the molten pool. Increasing the depth of the molten pool could inhibit the floating of inclusions to the surface to form slag. Increasing the content of the surface active element S that could change the surface tension temperature gradient could make the surface tension temperature gradient of the molten pool positive, thereby forming a deeper and larger weld molten pool.

       

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